Heres an update on the shootout motor,Eric who owns the bike has continued running around on it doing his wed night ride outs as well as a run up to cadwell park but has been a little lost as to why its so tractable and felt more could be had as he reckons a std ts1 is more peaky
so he stripped the motor out and sent me the top end over for a rework whilst he gave it a once over following its torture at elvington doing over 55 runs up the strip
he found the chain stretched and in need of adjustment and thought he would try it with a close ratio box,he found the clutch had started to slip so fitted new plates and heavier springs along with some new gearbox bearings that showed some wear
i set about the barrell based on the high bmep figures ive seen on the 225ts1 at 39bhp it led me to believe that although this 250 was powerful it still wasnt as efficient so had more power potential left in it,making some changes to port durations to help improve blow down and trimmed the piston cut outs to match the cylinder better
the straight line ignition has been swapped for a varitronic and just thrown on to be fine tuned on the dyno to find best results
collected it today and eric took it for a quick spin and reports no loss in tractability

but feels a lot quicker so see what the dyno says
i dynoed it on same jetting as a previous dyno run on a middle of the road jet and have yet to fine tune the varitronic timing to find best results which i hope to do tomorrow
so heres the graph before and after ,didnt think id find this much more especially with no major low down losses so still leaves more to try
i need to dial the ignition in then revert back to old ignition to see if this is where part of the improvement has come from
b4 40.64 bhp
after 45.52 bhp
