Got the motor back together and everything looks really good. With as much one-off fabrication involved as this project has, it's hard to decide how far to take something without knowing if it will work or not. I think that's one of the biggest factors that went into the initial failure; lack of attention to the usual minutiae due to the unknown. It's hard to justify spending hours and hours on something that isn't going to work, so you have to decide when to "call it". At the end of the day, I'm surprised it all worked as well as it did and the fact that it seized on the dyno and didn't blow the bottom of the crankcase out doing 65mph is OK with me!
Needless to say, I'm embarking on Chapter Two, so to speak, and I'm approaching things as if they're going to work, paying careful attention to detail.
First off, I need to check the port timings, TDC, and the like...
TDC by
PotvinV8, on Flickr
TDC on mark by
PotvinV8, on Flickr
I added some timing marks so that I can strobe it once it's up and running and then program the MSD ignition to suit. Rotax specs call for 17-degrees initial and 24-degrees total, all in by 4,000rpm, so that's what I marked, in addition to TDC.
Timing marks by
PotvinV8, on Flickr
I also cc'd the combustion chamber to ensure we didn't make the same mistake as last. The combustion chamber volume came in at spec, 28cc, so all's well. I also checked the squish and that was within spec too. Things are looking good!
CC head by
PotvinV8, on Flickr
The motor is back in the bike and I'll be concentrating on sorting out the exhaust next. I have a KTM300 FMF pipe that I'll be using as a base, along with a few specs pulled from various sources for comparison. Hope to be making blue smoke again very soon!